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authorJonathan Cameron <Jonathan.Cameron@huawei.com>2020-09-20 14:27:38 +0300
committerGreg Kroah-Hartman <gregkh@linuxfoundation.org>2020-12-30 13:26:16 +0300
commitd4911cdcd3576089d874b11040320e05071e57d6 (patch)
tree92e9b22313eb79adedcea787f62be71f9e82439f
parente4c3573b76a2665f4a09447e7f58125292ed3768 (diff)
downloadlinux-d4911cdcd3576089d874b11040320e05071e57d6.tar.xz
iio:imu:bmi160: Fix too large a buffer.
commit dc7de42d6b50a07b37feeba4c6b5136290fcee81 upstream. The comment implies this device has 3 sensor types, but it only has an accelerometer and a gyroscope (both 3D). As such the buffer does not need to be as long as stated. Note I've separated this from the following patch which fixes the alignment for passing to iio_push_to_buffers_with_timestamp() as they are different issues even if they affect the same line of code. Signed-off-by: Jonathan Cameron <Jonathan.Cameron@huawei.com> Reviewed-by: Alexandru Ardelean <alexandru.ardelean@analog.com> Cc: Daniel Baluta <daniel.baluta@oss.nxp.com> Cc: <Stable@vger.kernel.org> Link: https://lore.kernel.org/r/20200920112742.170751-5-jic23@kernel.org Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
-rw-r--r--drivers/iio/imu/bmi160/bmi160_core.c4
1 files changed, 2 insertions, 2 deletions
diff --git a/drivers/iio/imu/bmi160/bmi160_core.c b/drivers/iio/imu/bmi160/bmi160_core.c
index c85659ca9507..e95d817c8390 100644
--- a/drivers/iio/imu/bmi160/bmi160_core.c
+++ b/drivers/iio/imu/bmi160/bmi160_core.c
@@ -385,8 +385,8 @@ static irqreturn_t bmi160_trigger_handler(int irq, void *p)
struct iio_poll_func *pf = p;
struct iio_dev *indio_dev = pf->indio_dev;
struct bmi160_data *data = iio_priv(indio_dev);
- __le16 buf[16];
- /* 3 sens x 3 axis x __le16 + 3 x __le16 pad + 4 x __le16 tstamp */
+ __le16 buf[12];
+ /* 2 sens x 3 axis x __le16 + 2 x __le16 pad + 4 x __le16 tstamp */
int i, ret, j = 0, base = BMI160_REG_DATA_MAGN_XOUT_L;
__le16 sample;